In 2025, a municipal customer of Water Well Solutions (WWS), a licensed AirBurst partner, sought options to complete abandonment of a drinking water well. Per the Wisconsin Department of Natural Resources (DNR) regulations, the well owner and contractor must attempt to remove the casings completely before trying methods such as perforating and grouting. When all other methods were exhausted to try to remove or perforate the casings, WWS turned to AirBurst "AirXtraction" to enable the casing extraction, allowing WWS to complete the abandonment per DNR code.
The WWS team quickly brainstormed additional options. They did not have timely access to any perforating methods that could penetrate the 0.5” thick
Schedule 80 steel casing, and explosives were not permitted on this site. The team would have to try additional methods to extract the casing. The team then improvised a way to significantly multiply the amount of lifting force they could bring to bear by
employing two external jacks to use in concert with the rig. However, even with a combined 240k pounds of lift capacity, the casing would not budge.
With the word “no” not part of their vocabulary, the WWS team called in some air support. AirBurst Well Services Chief of Operations, Mike Yakich, proposed hitting the casing with a limited set of 2,000 PSI bursts, starting where the screen and casing meet. Mike employed one of our largest airgun sets, the 1900LL airgun tool with 200 cubic inch chamber, to deliver maximum energy. The theory was that the AirBurst shock waves could first break up the mineral scale and biological growth that had accumulated in between the casings, enabling the team to then lift the casing out.
After only five bursts the casing moved in response to pulling a quarter of an inch, the first upward progress the team was able to make. On the sixth shot, the team was finally able to lift the casing completely using only the original R15, no supplementary jacks needed. Proceeding in 10-foot increments of casing, the WWS team was then able to complete the extraction and proceed to finish the abandonment scope per DNR code.
Problem Solving: The WWS and AirBurst teams took a “first principles” approach to understand why the traditional methods for casing extraction were not working. With a clear understanding of the root cause of the problem, they were then able to successfully improvise on the fly.
More than just rehabs: AirBurst is a flexible technology that can be applied to more than just simple mechanical well rehabilitation jobs. Find out about our entire family of services here
Contact AirBurst Technology today to learn how we can restore your well's performance or help in those tricky situations.